Vaillant Ecotec plus 624 repair
This is a quick overview of the procedure I followed to replace a leaking main Heat eXchanger (HX) in a Vaillant Ecotec plus 624 system boiler. (the procedure would be much the same for many Vaillant boilers made in the last ten years or so).
This is not intended as a primer in boiler repair. It is assumed that you are competent to do this kind of work and have the required skills and tools. If in doubt call a professional! See the Boiler repair article for more guidance.
Over a period of time the central heating system had been showing slow pressure loss. This had got to the point were a litre or more was being lost per day. This is obviously not good, since it could mean loss of water into the fabric of the house and the possibility of supporting dry or wet rot, or damage to decorations etc. Its also not good for the heating system since one is introducing fresh water all the time, and hence more oxygen (so more corrosion) and hard water scale.
Hunt the leak
There were no stains on the ceilings downstairs, so it seemed unlikely it was the upstairs radiator piping. Checking things like the drain point outside and also the pressure relive blow off pipe for leaks (small plastic bag fixed over the ends), again found nothing. So then, several days spent getting under the downstairs floors, creeping around the crawl space, and ... nothing - it all looked good.
So with a bit of thinking, that only left the boiler itself. There was no obvious water near that, however being a modern condensing boiler there is one place it can leak and not be obvious - inside the primary heat exchanger. Any loss there will be directed into the condensate drain. So I turned the boiler off for a couple of hours, and emptied the condensate trap. A bit later the trap was half full again! (it should only fill when gas is being burnt). There was also some discolouration of the plastic of the trap, which is also unusual - normally the water is here is crystal clear. Taking the trap out altogether, revealed a small drip every few seconds or so.
So we have a culprit, now all we need is some warmer weather!
I found a really good local(ish) company that had the right reconditioned part in stock (it seemed excessive putting a £400 new part in a 7 year old boiler). The were also able to advise on the exact part needed, and quickly fixed an omission from the order with no fuss and next day delivery. For the fix I needed the HX itself, plus a new main gasket for the burner (needs replacing every time you remove the burner) and the kit of extra bits like the nuts for fixing the burner (also need replacing every time since they have a "one time only" insert to lock them in place). Plus other washers etc as might be required. (The seal and fixings etc usually all come together in package as Vaillant part number 0020038679)
This is relatively straight forward if taken step by step. Aided by a very good internal design and parts layout. However it makes sense to take lots of photos of connections and wire routings etc in case you need them for reference later.
Isolation and Draining
For this job the boiler needs to be drained (although not the whole heating system), power turned off, and the gas shut off. The valves on the bottom of the boiler where the pipes enter will allow all services to be turned off, and also there is a drain point for the boiler itself).
Slackening the single screw on the bottom edge of the front panel allows that to be removed once the two metal spring clips are depressed to free the panel. That then lifts off the top of the case. You can also pull the plastic decorative cover plate off the base of boiler at this stage.
(Click pictures for larger versions)
First remove the plastic air duct - this is a push fit into the burner / fan assembly, and is retained by a single screw into a bracket at the top of the boiler.
Next taking of the left hand side panel (two screws, one at top and bottom) makes access easier.
Also the expansion vessel can be removed - undo the single union nut at the inlet pipe, and remove two screws on the very top of the boiler to free to top retaining bracket. The part then slides forward.
Next disconnect the wires to the burner fan assembly, and also those to the HX itself; the ignition feed and earth wire, and the connection to the fusable link at the top of the HX (these HX have a emergency fuseable link to prevent a catastrophic melt down should the boiler fire for any length of time with no water in the HX).
Now disconnect the union nut on the flexible corrugated gas inlet to the burner.
Finally, remove the burner by removing the 4 retaining nuts on the face of it. The whole burner assembly will now pull out of the HX and can be placed safely aside.
Next we need to free the HX from its pipework. There is a hose clip on the flexible plastic hose to the condensate trap. Loosen this, and pull the pipe off the spout. You can also pull the pipe from the condensate trap, and set that aside.
Next the main CH feed and return push fit connections need to be freed. First remove the metal retaining clips on the base of the HX. These pipes will usually have a little wiggle room, and you can pull them free slightly at this stage, even if not get them out completely.
Now the main HX itself can be removed (take care, its heavier than it looks). Undo the retaining nuts in the clips at the front. For ease of access I also unscrewed the retaining brackets from the back wall of the boiler as well. You now need to rotate that whole HX a little bit clockwise, so as to simultaneously pull the pipe connections up off the feed and return pipes, and also pull the main flue connection down from the flue terminal spigot (also a push fit). Once free the HX will come out.
You can also remove the condensate syphon at this stage for cleaning. First withdraw the trap from under the boiler with a partial anticlockwise twist to unlock it, then pull it down and out. The syphon itself can be freed from the base of the boiler by pushing in on the three retaining lugs under the boiler while pulling it up. Lastly you need to wiggle the syphon out of the boiler (this is the one slightly sub optimal bit of design since you cant simply lift it up as the pipe to the pump is in the way). I found that by rotating it 90 degrees anticlockwise, and then prising it leftwards behind the pump, it was possible to free it. Note if doing this on one of the 800 series combi boilers, its probably just simpler to disconnect the pipe to the pump, since the secondary hot water HX will be in your way on these models).
There are a couple of service jobs that can be done at this stage. The first is to sweep any dust and loose stuff from the outside of burner itself with a soft brush.
Next remove the old graphite impregnated steel mesh seal around the rim of the burner assembly by prising it out of its channel. If it has stuck to the channel at any point then carefully scrape the channel clean so the new gasket will seat correctly. Fit the new gasket, by carefully pushing it into its channel as you work around the rim.
Since CH primary water had been getting into the condensate drain and syphon, I also gave the pipe and syphon a thorough clean - rinsing through and shaking out the closed section several times, while also using a pipe brush on the more accessible bits.
I also checked the pressure in the expansion vessel - spot on the value (0.4 bar) shown on its label.
I carefully wiped round and checked the 'O' rings on the main feed and return connections to the HX, as well as the flue connection on the new HX and made sure the matching flue spigot in the boiler itself was also clean. A little silicone grease can aid assembly.
The CH system has a Fernox TF1 magnetic / cyclone trap fitted, so I drained and cleaned this.
In true "Haynes Manual" tradition, this is basically the reverse of the above.
First I replaced the condensate trap - wiggling behind the pump and twisting into place.
Before refitting the main HX, I connected the lead to the fusible link connection on the top, since this would be harder to reach once in place.
Once the HX is pushed onto the flue spigot, and down onto the push fit pipe connections, you can replace the brackets and fix it in place, and refit the clips that retain it from the front.
Now replace the spring clips that lock the feed and return pipes in place.
Push the condensate pipe onto the spout on the bottom of the HX, and tighten its clip. Push the other end into its connection on the syphon.
Now replace the expansion vessel, and refit its retaining clip. Reconnect the union nut at the bottom, taking care to make sure you have included the fibre washer.
Now refit the main burner assembly. This is retained by the 4 nuts on the face of the burner. Remember to refit the bracket that holds the air duct under the top right fixing. The nuts have a positive end stop when tightening.
Remake the gas connection to the burner, using a new fibre washer from the kit of spares that come with the main gasket.
Now remake all the wired connections to the burner / fan assembly, and also the main HX itself. (note the installer manual for my boiler does not actually match the reality in this case since it describes two connections only on not the five it actually has, however the connections are keyed and mostly colour coded - so its pretty much impossible to get them wrong)
Lastly refit the air intake duct and fix with its single screw.
Recommissioning / Testing
Refill the condensate trap with clean water, and fit back into the syphon. Make sure to check that it reconnects to the condensate drain pipe under the boiler, or you may end up with a wet counter top later (DAMHIK).
Now turn on the gas service valve, and check the connection to the main burner is gas tight with some leak detection spray.
Turn on the feed and return service valves, and ensure there are no leaks from the connections to the HX.
Next I opened the CH drain point a bit, and refilled at the service loop - this allowed all the air to be pushed out of the boiler. Then I closed the drain point. Next I set the system pressure to be "adequate" using the small internal pressure gauge (you can't see the more accurate digital one until the unit is powered).
To be sure that the boiler was properly bled of air, I turned off the gas inlet tap to make sure it could not fire, and powered on the boiler. Pushing the flame stop button early on in the power up, prevents the boiler from trying to fire (and even if it did, there is no gas anyway, so it would lock out with an ignition failure code). Now enter the "installer mode" from the menu on the boiler's control panel, enter the installer code (typically 17 unless you have changed it), and go into the test programs menu. Selecting program P.0 will enter the "Bleeding test program" - i.e. it will just run the pump. Now you can set the system pressure and bleed all the rads etc (even if not fully drained there is a fair chance there is air in the system just because of the leak). Once fully purged of air, I shut it all down again, and turned the gas back on. This time allowing it to do its normal "proving" and ignition on power up. So far so good. Then since it was a very warm day and there were no heating demands, I used the test programs to run the system first on minimum load, and then full load. Again checking for any leaks or unexpected behaviour.
Once everything looked good, I replaced all the casing, and leave it back in normal operation.
Final tidy up
After a couple of days the system pressure was still good, so no more leak! I added fresh fernox x100 inhibitor to the system (using the TF1 as a handy place to pour it in ( you need a couple of goes to get the whole 1L in there)).
Interesting to look at the failed HX:
Plenty of hard water scale on there from the leaking primary CH water. Hard to see any exact failure point however. Since a trip to the tip was beckoning, and life is too short to waste much time identifying the exact failure its not easy to tell what caused the initial problem after only 7 years on a system that was well cleaned and has been well maintained with inhibitor etc. Ironically the salvaged replacement part used was actually two years older than the original.
The boiler's rating plate. Note there are a number of variations of this boiler - especially in the suffix after the final "/":
and the main Giannoni HX - as used in many makes of boiler and across the Vaillant range. The GM30-45 bit seems to be the important part or the nummber, the 006-13 seems to vary a bit. The 24kW boiler uses the version with 5 parallel water loops, the lower powered ones have the slightly less deep version with only 4. (its the parallel paths that make it very difficult to flush blockages from these HX).